Risk of running into a 'my month was worse than yours' threadjack. Reminds me of this pre - Monty Python version of the 4 Yorkshiremen .
https://www.youtube.com/watch?v=VAdlkunflRs
https://www.youtube.com/watch?v=VAdlkunflRs
Time to update this tale: I’m back on the road again – well sort of – DMV lost my registration renewal and my plates are 7 months out of date. Denver cops really don’t give a damn about registrations during COVID19 so I’m driving it anyway.
Low compression pistons? Are you planning on adding boost?
Quick update: I finally got a 1000 miles on the new engine after making many data logging runs on Maps 1, 2 and 3, Part Throttle, EGR and Power Enhancement. The pulse width and AFR outputs are very close to a very steady 14.7 AFR for maps 1 and 2. If it ain’t broke, don’t fix it –or even try to fix it.
Map 3 results were quite rich on both Brian and John’s ECU bins, and I’ve make about 6 different bins to get the AFR right at ~12.75 during Power Enhancement.
I’ve spent a LOT of time creating a small Visual Studio/Excel application that rapidly separates and graphs the data logging run into useful visual results. I’m in the final process of bundling this application into a Setup file that I’ll post on John Powell’s Google Docs account when done.
Some times when data logging, the logging dashboard indicates VTEC is on even at idle, which is obviously bogus. After driving a little bit the gauge seems to reset itself, and I have not pursued the (non) issue. But now it may be more of a concern.
I’ve check the ground connection as the first part of the manual’s trouble shooting procedure, which is about a far as I can go without the test harness. More important, I’ve changed the ECU bin back to the
Brian’s original bin and the car behaves the same. I’m thinking mechanics and not electronics. Two of my Denver friends have their engines in various states of assembly/disassembly so perhaps I can borrow an oil pressure switch and test again. It is more than possible that a small bit of assembly debris could clog the screen filter on the switch and simply cleaning it will solve the problem.
Suggestions appreciated and I’ll keep you posted.
Since the motor isn't even a year old and only has 1000 miles on it I don't think there's a need to replace the VTEC solenoid gaskets unless they are leaking. The gaskets are rubber and will work as long as they are still stretchy and pliable, and the grooves limit the squish so they aren't ruined after installation. Once the issue is resolved it might not hurt to replace them for peace of mind but during troubleshooting that seems like a waste of good parts. I've removed and reinstalled VTEC solenoid gaskets multiple times with no issues.
Edit: Fun fact, most of the gaskets on the motor in my car now came off the failed built motor that had 400 miles on it, they all looked indistinguishable from new parts so I just transferred them all over. (There were a couple exceptions like the oil pan gasket.)