Before I do anymore changes I want to ask opinions on what may be the issue for this right now. Here's the background of my kit.
Custom made by member Elite
Precision 6262 turbo
Tial BOV
Tial 44mm Wastegate
Manual boost controller
A2A inter cooler
500whp, 93 octane, and a boost spike up to 16psi which then settled down to roughly 14 if I remember
Now the important things I recently changed
Manual boost controller to an electronic one "mac valve"
SOS W2A inter cooler
My issue is with boost creep now. I don't have the dyno sheets or logs but once I set up a laptop I can pull some runs and post but we ran the car on the dyno and after slowly turning the boost up or doing what tuners do with the valve we reached 14psi. I was running some not to good gas that I got in the corn fields of maryland but didn't think much of it and we heard some slightly knock so we just turned it back down to 12psi. At 12psi we did 477whp which I'm happy with. We also set up a triggered toggle switch on one of the pins to activate and deactivate the mac valve so I can just run wastegate spring pressure for the track.
We tuned on Monday evening. I had VIR Tuesday and Wednesday and only ran the wastegate setting. Thursday I switch back over to activate the mac valve and the car seems to let off under WOT pulls.
I test this out and it happens in 2nd and 3rd gear pulls and I didn't try the others. After meeting back up with my tuner he pulls some logged runs today and we discover that it's creeping up. I believe we set it at 13.66 for cut off but the target was 12psi.
I'm just wondering what it is? A key thing is that the car ran fine and I didn't notice anything at VIR this past week when I was just running wastegate spring pressure. I was WOT on the straights as well for the most part in 3rd gear and had no issue or cut off. Essentially these items are all the same as well when I had my previous tune on the manual boost controller, the items are all the same size... It's really odd because when he was tuning the car it didn't behave like this on the dyno either. I didn't hit anything at VIR, and the only thing that I'm told to check is the lower wastegate line to make sure that doesn't have holes or damage, but I ran the lines away from hot items and I don't think that's the issue.
So the theory is that since I was running higher boost before the creep wasn't an issue since we were running more boost. Now that we're trying to limit it lower the wastegate can't let enough pressure out therefore we need a larger waste gate "my tuners saying a tial 60mm wastegate would work".
Another option is to run good quality 93 octane gas and hope to not knock and go back up to 16psi target
I'm kind of stumped. Spark plugs were changed and gapped low. I believe they are Ngk 7's and gapped at 22. I clocked my turbo when changing things out and also had the turbo itself off the Y pipe and the wastegate off. I'm just trying to list things that I had my hands in too just encase I should check anything specific out.
Other then that I'm stuck with trying to throttle enough to run hard but not enough to go into boost creep.
Custom made by member Elite
Precision 6262 turbo
Tial BOV
Tial 44mm Wastegate
Manual boost controller
A2A inter cooler
500whp, 93 octane, and a boost spike up to 16psi which then settled down to roughly 14 if I remember
Now the important things I recently changed
Manual boost controller to an electronic one "mac valve"
SOS W2A inter cooler
My issue is with boost creep now. I don't have the dyno sheets or logs but once I set up a laptop I can pull some runs and post but we ran the car on the dyno and after slowly turning the boost up or doing what tuners do with the valve we reached 14psi. I was running some not to good gas that I got in the corn fields of maryland but didn't think much of it and we heard some slightly knock so we just turned it back down to 12psi. At 12psi we did 477whp which I'm happy with. We also set up a triggered toggle switch on one of the pins to activate and deactivate the mac valve so I can just run wastegate spring pressure for the track.
We tuned on Monday evening. I had VIR Tuesday and Wednesday and only ran the wastegate setting. Thursday I switch back over to activate the mac valve and the car seems to let off under WOT pulls.
I test this out and it happens in 2nd and 3rd gear pulls and I didn't try the others. After meeting back up with my tuner he pulls some logged runs today and we discover that it's creeping up. I believe we set it at 13.66 for cut off but the target was 12psi.
I'm just wondering what it is? A key thing is that the car ran fine and I didn't notice anything at VIR this past week when I was just running wastegate spring pressure. I was WOT on the straights as well for the most part in 3rd gear and had no issue or cut off. Essentially these items are all the same as well when I had my previous tune on the manual boost controller, the items are all the same size... It's really odd because when he was tuning the car it didn't behave like this on the dyno either. I didn't hit anything at VIR, and the only thing that I'm told to check is the lower wastegate line to make sure that doesn't have holes or damage, but I ran the lines away from hot items and I don't think that's the issue.
So the theory is that since I was running higher boost before the creep wasn't an issue since we were running more boost. Now that we're trying to limit it lower the wastegate can't let enough pressure out therefore we need a larger waste gate "my tuners saying a tial 60mm wastegate would work".
Another option is to run good quality 93 octane gas and hope to not knock and go back up to 16psi target
I'm kind of stumped. Spark plugs were changed and gapped low. I believe they are Ngk 7's and gapped at 22. I clocked my turbo when changing things out and also had the turbo itself off the Y pipe and the wastegate off. I'm just trying to list things that I had my hands in too just encase I should check anything specific out.
Other then that I'm stuck with trying to throttle enough to run hard but not enough to go into boost creep.