The AC project is in the bag. I finally got the right part, and got it all back together and charged up this weekend. [emoji3587][emoji3587]
For context, what was my AC problem? After
some thrashing initially to get it converted to R134a and working by a shop, it appeared that the compressor was bad. All goo all over
My assumption was that the compressor was not able to hold a seal somewhere, and it had leaked all the refrigerant out. The solution would be a new compressor and some new o-rings at the compressor. Seemed reasonable enough.
But when I went to remove the compressor, there wasn't, uh, an egregious leak. I suppose there was just not enough pressure to kick the compressor on.
With the compressor out, it was pretty clear that the source of the leakage was the pressure relief valve. See the green here:
Prior to seeing it in the flesh, I didn't even know this part existed. Basically it's an over-pressure failsafe. It's hooked up to the high side (discharge side) of the manifold block. Pressure over like 350psi? Open! Newer cars don't even have these things as it's not ideal to vent to the atmosphere, they shut the compressor off in an over-pressure situation instead.
The question is why. Why did this valve open in the first place? After some reading, here are a couple potential reasons:
* The valve it self was bad. It's possible there was an over pressure situation in the past and made it open even at lower pressure. Maybe it just went bad? Seems unlikely though.
* There could be a blockage somewhere in the system.
* It was overcharged?
* Some issue with the compressor?
I could sorta address all these things by replacing the compressor, the valve, flushing the system to make sure there is no blockage, then properly charging it.
The valve
Ok so I needed to replace the valve. This section is kinda long because this was the most painful part of the whole job. This dumb little $10 part is the reason the car was in the air for 3 weeks.
The stock 91 relief valve (38801-PT3-A01) is, like all the other R12 specific parts, discontinued. Well, what about the later-model one? I was trying to finish the job the day I discovered that I needed to replace the valve.
I called around and the local Acura dealership had the late-model part (38801-P9K-E01). It was $78 and like 1/3 the price on Amayama, but I needed it so I went and happily overpaid so I could finish the job.
Does it fit? Nope! The threads in the manifold block are totally different:
* 91-92 R12 - 3/8"-24
* 93+ R134a - M10x1.5
So I needed either a manifold block from 93+ car with the M10 threads or a valve with 3/8"-24 threads.
I tried to find a manifold locally, but nope. The best option was Amayama, but their lead time is often several weeks to a month.
Ok, maybe an aftermarket valve? With an aftermarket valve, there were other considerations beyond thread size. First of all, I needed valve with a "non-captive" o-ring. There is a recess in the manifold housing for the o-ring, so the valve can't have one
Aaand the last consideration is that some valves with the correct threads and o-ring configuration explicitly said "only for R12". Ugh, why? I read it may be that the max pressure is higher for R134a. It is possible that it was only because of the o-ring used. But I didn't want to risk it, only to have to tear everything apart later because of this dumb thing. I wanted to find a valve that indicated it'd work with R134a.
This was also a process, many websites that list these have pretty minimal info. What are the threads? Is it a non-captive o-ring? Is it for R134a? Napa had one, I ordered it and picked it up: captive o-ring, not it.
After tons of searching, I landed on Sanden T6951 / Airsource 5686A. It allegedly had the right attributes, and looked similar to the later OEM one. I bought two cause shipping was $18 for a $9 part. It finally came 3 weeks later:
Does it fit??? OMG Yes! Installed in the manifold block:
Everything else can go back together now!
Flushing
Moving on! Alright. I referred a bunch to
@Big McLargeHuge's AC post for this. I focused on flushing things on the high side: compressor to condenser line, both condensers, the line between the condensers, and the line from the condenser to the drier. If the lines were super dirty, then I'd do the other 2 lines, which are hard to flush because of the way they mount to the firewall.
I bought this four uncles flush kit:
I wanted to be super clean so I bought some plastic tubing, an oil mat, and had some leftover water jugs to collect the solvent.
3/4" ID tubing and a short piece of 1" ID tubing covered all the fittings just right:
I flushed the lines first cause they seemed easier. They were all very clean. Cool, onto the condensers.
The drivers side condenser was easier to deal with because of the angles IIRC, so I did it first. It was dirrrrttttyyy, wow. But I flushed it until clean solvent came out. There was no blockage here, just dirty.
Then I went to the passenger side. It seemed like there was indeed a blockage. At first virtually no air or solvent came out the other side, then all of a sudden it did, all at once. It happened very fast, it's possible I had the spray gun at a weird angle or something at first. Or you know, there was an actual blockage. A plugged condenser, especially the first one from the compressor could explain an over pressure situation.
Here's the jug after flushing the drivers compressor, it's v dirty. You can also see the short 1" tubing. It slides over the 3/4 tubing for the big fittings:
A couple things I learned while flushing the system:
* The solvent flush gun will use all the solvent you put in the canister within 2 seconds of pulling the trigger. The canister holds a lot so you can go through a ton of solvent very quickly. I only bought 2 cans of solvent. I spent a lot of time filling the canister 1/4 of the way to conserve. Pull the trigger, is it clean? If not, run another 1/4 can through the part. I used about a half a can for each condenser. I ended up a little of the 2nd can of solvent left.
* The fittings on the flush gun would bust loose on occasion while under pressure and spray solvent everywhere. It's tough to get the canister (upright) and spray gun (contorted) oriented correctly, so there was a lot of moving and twisting. Sometimes the twisting would break the fittings loose. I learned to hold onto the fittings when moving the flush kit around. Also wear goggles omfg
* After flushing, especially the condensers, there was a bunch of solvent still in the part. I just blew air through them until they were dry.
The compressor
There are several options for the compressor. Which compressor? Which oil?
I made
the decision a while back to use the 91 replacement compressor (Denso 471-1424) and ester oil for ease and compatibility all around. I get a new pulley and clutch, don't need to replace the bracket or connector, and I'll load it with oil that is compatible with the small amount of residual mineral oil in the system. If I were starting with all new parts, I'd go with the 97+ compressor, PAG oil and related parts. But I'm not, so 91 replacement + ester it is.
First up was draining all the oil out of the new compressor. It's mineral oil, and I wanted to get as much out as possible. I had a bit of a hard time getting the oil out and measured. It was pretty cold when I was doing this (in the high 40s), so it's possible it was higher viscosity than in a normal situation. I got about 40ml out and measured:
I was having trouble getting more out quickly, so I just left it upside down for a while, rotating the pump every now and then. I probably got another 30 or 40ml out of it that way.
I would be flushing a few lines and the condensers. I loaded it with 100ml of ester.
Cool. I got new o-rings and a new idler
Then everything installed and the belt back on. Yay!
Reinstall
Overall, reinstalling everything went smoothly. The epoxy on the motor mount nut broke loose, but I was able to get both hands in there and get it connected. I was even able to get the torque wrench on it.
Here's the torque spec page for the crossmember and friends cause I didn't take any pics. I like torquing suspension parts.
Car on the ground
Finally I could put the car on the ground. I started it up to make sure there are no oil leaks from all the oil work I did. No leaks! So far. We'll see after some driving and trips up to redline.
Drier
I bought a four seasons 33412 drier. I also got a new bracket cause mine was rusty and I read that the later drier was smaller. We'll this drier is a pretty fat boi, so I had to get a new like 50mm bolt. Titanium cause why not:
Then right before pulling vacuum, I installed the drier and connected up the lines.
Pulling vacuum
Next up was pulling vacuum. This will remove moisture in the system and tell you if there are any leaks. Like can it hold vacuum for 30 minutes? If so, no leaks.
I got this little thing
Then I hooked up my AC gauges.
Connected the air compressor with the engine off, opened all the valves, and we had vacuum.
My air compressor is a pretty little one ("the tank"). It would allow the pump to pull 25" at first, then when the tank was depleted, it'd only pull 23". Seems fine as long as it's under 20"?
I pulled vacuum for 15 min, closed the valves, then disconnected the compressor to make sure it held vacuum. I waited for about 30 min, and the gauges didn't move, so I figured it was fine to go ahead and start the charging process.
Before charging, you pull vacuum _again_, but for longer. Hook up the vacuum pump again without the car running, and plug the compressor in. I think I pulled it for about 45 min. The annoying part is the air compressor is running the entire time. "Why is it so loud out there?" my girlfriend asked several times. Progress, you know?
It seems like it removed a bunch of moisture. I put a rag under the pump and it was pretty soaked at the end.
Charging
I watched this video below and it jived with everything else I had read:
https://youtu.be/Pdq8JAlct6s
I measured all the cans. I was shooting for a tiny bit over 800g. My cans had about 330g of refrigerant in each.
I didn't get any pics while filling. And the video does a great job on the steps, so I won't rehash here. But there were some things I learned:
When you add the first can, there will be air in the yellow fill hose. You need to vacate air from the yellow fill hose so it's only refrigerant. I had no Schrader valve on the fill hose or my gauges. Before I opened the low side valve to start the charging, I burped the yellow line fitting at the gauges. In this pic, I would loosen the yellow line fitting until some refrigerant came out, then tightened it back up:
* I had trouble swapping in a new can. In the video, he swaps it out with the valve fully closed to hold Freon in the fill line. When I tried that, refrigerant went everywhere. I ended up just burping the fill line each time.
* After the first can, AC Compressor didn't consistently stay engaged. This is probably normal, but I dunno. It'd stay on for 10-20 seconds, then kick off for 20 seconds, kick back on, etc. Maybe cause ambient was cold? It was high 50s F in the garage. It'd only pick up refrigerant when the compressor was engaged, so it took a while.
* When I was finished and with the compressor engaged, the low side ended up being 25psi, high side was 148psi which is in line with all the charts for my coldass ambient temp. I ran it for a while after charging just to make sure those pressures were consistent over time.
* I ended up using 810g of refrigerant. Though, there may be less in the system as a bit came out while burping.
Done!
We'll that's it! I have AC finally! It's cold! Everything seems to work (condenser fans etc)! I’ve had the car up in the air again a couple times, and it seems like no leaks. Hopefully it lasts this time. I'm really glad this project is over.
I also made progress on the oil temp sensor. I’ll post about it soon