AWWWW NOOOOOOOOO
How were you driving it when it happened? Please share some more details.
Really sorry that this has happened. Don't give up, make your nsx great again! #mnga
Car wont even turn over now.:-(
Yep. I just got off the phone with Shad. Most likely a blown piston which pressurized the crankcase and blew out the dipstick. At 10k for a motor rebuild, I might just sell it as a project car.Expensive repair like I said.
My crankcase pressure built up and pressure pushed my dipstick out before I noticed anything. Another reason why I took my engine cover off.
That would be a sight to see....Don't sell it. Do the conversion that some others are doing.
It sucks to grenade an engine. I did it on a boosted Saleen and the rod went through the side of the block. It was impressive!![]()
Thanks Kenny. I blame my newly acquired vanity plates. Never had custom plates before and first ride with them, KABOOM!!! It needs to read BLWNC30 now.....My deepest condolences![]()
But for now its either go big or go home.
Thanks. I appreciate the support. I really do not see myself selling the car especially for about 15k I imagine to get it to how I want it, that is Kia sedan money. But on the other hand, the paint is starting to get really knarly and the brakes/abs would be a liability as well. Which would probably put that 15k number well into 30k. But still, for 30k there is absolutely NOTHING I would purchase as a replacement. So, it just might be time to hunker down and just do it. The car is free and clear, was bought as a stolen/salvaged vehicle for 16k....https://www.scienceofspeed.com/index.php/nsx/enpp/engine-services/fi-custom-engine-program.html
https://www.scienceofspeed.com/inde...ofspeed-twin-turbocharger-system-for-nsx.html
This is big !!
Jinks , I'm truly sorry for your loss. I know the feeling of sick to stomach, vomit , cold sweats & the thought of just passing out when the shock overwhelms. Again , best to you and hope you stay in the NSX game.
If I am moving back to Florida this coming year yes. But I would opt for the K20 turbo. If staying in California, no. I cannot boost it. Besides, Shad still has a race spec comptech motor sitting in the shop that was meant for Rob's track car before it got totaled, who knows. First things first is find cause then decide a solution. For all I know, my fuel pump could have failed or maybe it was in fact just a bad head gasket. But I concur with the fact that the dip stick flew out of the crankcase as a blown piston or rod which Shad and SDuff has mentioned. It's just a shitty ass situation anyway you slice it.Are you SURE you wouldn't consider a J-swap? Cheaper and ability to make the same, if not more, power for less money....
Under full boost. Whipping the shit out of a 5.0 mustang. Then just a loss of power, oil light and check engine light. Engine bay full of vaporized water and oil. Thinking maybe just a gasket. Can't even sleep now. I hope it is a gasket. My poor car is just littered in oil. Even blew the dip stick out of the motor.